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Cessna 206 Stationair (N3800G) - Aircraft crashed in 2004. Photo taken in 1993 during a Florida trip: The airline transport certificated pilot was flying passengers and a cameraman associated with a film production to film a fort on an island. During the filming, the pilot stated he switched fuel tanks, and noted that the left tank was full, and the right tank about 3/4 full. As the airplane approached the fort, the engine sputtered, and then regained full power. A minute or two later, the pilot indicated the engine lost all power, and after unsuccessfully trying to restart it, he ditched the airplane. The pilot and passengers were all able to exit the airplane except the cameraman, who tied himself to the seat with a rope prior to takeoff after the cargo door had been removed to facilitate filming. Attempts to free the cameraman prior to the airplane sinking were unsuccessful, and he drowned. A passenger noted that the right fuel tank fuel gauge was somewhere around the 1/4 mark, and bouncing as the airplane flew. Postaccident inspection of the airplane, recovered 17 days later from ocean waters, disclosed no evidence of any pre-impact mechanical malfunction. CAUSE: A loss of engine power for an undetermined reason during cruise flight, which resulted in the pilot ditching the airplane in ocean waters.
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Cessna 206 Stationair (N3800G)

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Aircraft crashed in 2004. Photo taken in 1993 during a Florida trip: The airline transport certificated pilot was flying passengers and a cameraman associated with a film production to film a fort on an island. During the filming, the pilot stated he switched fuel tanks, and noted that the left tank was full, and the right tank about 3/4 full. As the airplane approached the fort, the engine sputtered, and then regained full power. A minute or two later, the pilot indicated the engine lost all power, and after unsuccessfully trying to restart it, he ditched the airplane. The pilot and passengers were all able to exit the airplane except the cameraman, who tied himself to the seat with a rope prior to takeoff after the cargo door had been removed to facilitate filming. Attempts to free the cameraman prior to the airplane sinking were unsuccessful, and he drowned. A passenger noted that the right fuel tank fuel gauge was somewhere around the 1/4 mark, and bouncing as the airplane flew. Postaccident inspection of the airplane, recovered 17 days later from ocean waters, disclosed no evidence of any pre-impact mechanical malfunction. CAUSE: A loss of engine power for an undetermined reason during cruise flight, which resulted in the pilot ditching the airplane in ocean waters.

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